Carolina Horsepower

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-   -   It done Broked (http://www.balatrons.com/forum/showthread.php?t=5409)

DolSVT00 03-29-2010 08:16 PM

It done Broked
 
Well its official, I hurt something. Not at the track, but on the way home from the track lol..... I know I lifted a head, but I think I have some bottom end problems too.........................

I bounced it off the limiter in the top of 3rd with the gun blazing, I'm pretty sure I had problem's already from another beating I put on it a couple months ago but this put the nail in the coffin....................

Zacharyx 03-29-2010 08:19 PM

sucks to hear

Dave 03-29-2010 08:28 PM

Sorry to hear this Randy, just when you were looking for long bars, now this....def. sucks.

Illusions 03-29-2010 08:31 PM

sorry to hear that Randy. I hate it when things break just when you think your all set to get back to the track and everything normal again. :(

Whaler 03-29-2010 08:41 PM

Sorry to hear that, Randy. That bites.

jmd 03-29-2010 08:56 PM

srry to hear. sounds like a rebuild and turbo time.

DolSVT00 03-29-2010 08:57 PM

Quote:

Originally Posted by Dave (Post 69100)
Sorry to hear this Randy, just when you were looking for long bars, now this....def. sucks.

Just baught a set too, I used them at the track this weekend. I can't blame anyone but myself for breaking it.......

DolSVT00 03-29-2010 08:58 PM

At least I Gapped that SOB.......................LOL

Pesce Nero 03-29-2010 09:03 PM

sorry to hear that Randy

chrisheltra 03-29-2010 09:08 PM

Quote:

Originally Posted by DolSVT00 (Post 69109)
At least I Gapped that SOB.......................LOL

vids or it didnt happen........

DolSVT00 03-29-2010 09:12 PM

Quote:

Originally Posted by chrisheltra (Post 69112)
vids or it didnt happen........

if you would have answered my phone call, you could have taken the video. I wasn't about to do it, I had my hands full.

I told the guy the website, maybe he'll sign up. His car was pretty damn fast.

04ctd 03-29-2010 09:12 PM

we slid the axle on one side last time.

was about $500 to fix it RIGHT.

and we were up till 1:30 friday (ok, actually Saturday AM) to be there on saturday.

hope yours goes smoother...but don't sound like you will come out cheaper..

chrisheltra 03-29-2010 09:15 PM

Damn dude I think I was still asleep when you called. Usually its the other way around.

CINDERBLOCK 03-29-2010 09:43 PM

ouch...

DolSVT00 03-29-2010 10:10 PM

Quote:

Originally Posted by 02_L#416 (Post 69125)
ouch...

Shit happen's, It shouldn't be a bad fix like last time I broke it and put a hole through the block lol.

I'm gonna pull it apart and look, but I'm pretty sure the piston's rods and block are still good.

CINDERBLOCK 03-29-2010 10:14 PM

Let me know if you need an extra set of hands.

slow04 03-30-2010 05:09 AM

Bummer...that thing was riding out good saturday

LXtasy 03-30-2010 07:23 AM

that sucks. i feel your pain. let's hope it is something simple

1iron 03-30-2010 08:48 AM

Good luck with the fix.

Matts94Z28 03-31-2010 12:51 PM

Randy, I actually know the guy you ran. He asked me about you on FB... I told him to join.

S130Z 03-31-2010 12:59 PM

Hey Guys!

My name is Adam, and sorry about the broken car man....I know how it feels. Randy, that thing is quick! Wish I had my front spoiler on when we ran, things got a little scary for me at 110+.

DolSVT00 03-31-2010 02:31 PM

Quote:

Originally Posted by Matts94Z28 (Post 69331)
Randy, I actually know the guy you ran. He asked me about you on FB... I told him to join.

Thats cool man, his car was quick..... Mine was already hurt, but that run put the nail in the coffin.


Quote:

Originally Posted by S130Z (Post 69334)
Hey Guys!

My name is Adam, and sorry about the broken car man....I know how it feels. Randy, that thing is quick! Wish I had my front spoiler on when we ran, things got a little scary for me at 110+.


Lil shakey for me too, I underestimated the car by looks alone the first couple times and let my tranny shift for me out of overdrive thinking it would be an easy kill.............

The last time we backed down I let her eat........

S130Z 03-31-2010 02:46 PM

Quote:

Originally Posted by DolSVT00 (Post 69348)

Lil shakey for me too, I underestimated the car by looks alone the first couple times and let my tranny shift for me out of overdrive thinking it would be an easy kill.............

The last time we backed down I let her eat........

:hysterical:I get that response WAY too often! Thats always my favorite thing to hear from people. I know, my car looks like crap :barf: (Man I love all these smilies!) The last run I let off early when I saw a huge mess of liquid pouring from the bottom of your truck. I had fun though.

DolSVT00 03-31-2010 02:50 PM

Quote:

Originally Posted by S130Z (Post 69359)
:hysterical:I get that response WAY too often! Thats always my favorite thing to hear from people. I know, my car looks like crap :barf: (Man I love all these smilies!) The last run I let off early when I saw a huge mess of liquid pouring from the bottom of your truck. I had fun though.

That would be when the HG let go, I bounced it off the limiter as I was coming by Waving instead of watching my guages LOL

S130Z 03-31-2010 04:48 PM

Yeah, being cocky can have its ups and downs. Are you running head studs?

DolSVT00 03-31-2010 10:39 PM

Quote:

Originally Posted by S130Z (Post 69377)
Yeah, being cocky can have its ups and downs. Are you running head studs?

Ya its built ARP's MLS gaskets bla bla bla, I most likely lifted it a couple months ago doing some testing with big pills. I was coming home from the track and had it loaded with a spare set of tires, Jack and some tools when we ran, all that weight plus the speed and slapping 6 grand caused it to leak, I still made it home and it drove fine temps were fine, but I lost about half my coolant in the resivoir and noticed a few bubbles at idle when I got home. I had been noticing level changes in the coolant for about a month so i'm certain the damage was already done.

No big deal, I have enough spare parts to fix it. I't shouldn't be down for more than a week or so. Motor's all but out already.

S130Z 03-31-2010 11:06 PM

Glad to hear man, hope everything goes smooth. Maybe some day we can have a re-match. Unfortunately, my fuel pump seized when I got back from charleston, and I had to put a new one in. You guessed it! Gotta re-tune all my tables, the new pump flows more than my old one. I went from a solid 12.0 AFR at WOT to a nice 10.0. At least it gives me a nice buffer when I turn the boost up to 12 psi sometime in the near future.

1iron 04-01-2010 07:23 AM

Quote:

Originally Posted by DolSVT00 (Post 69448)
Ya its built ARP's MLS gaskets bla bla bla, I most likely lifted it a couple months ago doing some testing with big pills. I was coming home from the track and had it loaded with a spare set of tires, Jack and some tools when we ran, all that weight plus the speed and slapping 6 grand caused it to leak, I still made it home and it drove fine temps were fine, but I lost about half my coolant in the resivoir and noticed a few bubbles at idle when I got home. I had been noticing level changes in the coolant for about a month so i'm certain the damage was already done.

No big deal, I have enough spare parts to fix it. I't shouldn't be down for more than a week or so. Motor's all but out already.

Engine out for head gaskets? That sucks!

chrisheltra 04-01-2010 07:38 AM

^^^ Yup

http://www.lightningrodder.com/forum...violent069.gif Cab forward design.

wade w 04-01-2010 05:43 PM

Quote:

Originally Posted by 1iron (Post 69477)
Engine out for head gaskets? That sucks!

Doesnt have to, but it is easier.

Lurch 04-01-2010 07:57 PM

Sorry to hear this!!
 
Sorry good luck on the new build !! Mitch

DolSVT00 04-01-2010 09:10 PM

Quote:

Originally Posted by wade w (Post 69553)
Doesnt have to, but it is easier.

Exactly, and if I'm that far and have it out I might as well replace the bearings and check out the cyl's.
Quote:

Originally Posted by Lurch (Post 69561)
Sorry good luck on the new build !! Mitch

Shouldn't be a new build, just the same old stuff and some new gaskets, it was running fine but it had a few bubbles in the overflow. I'm gonna try something different for gaskets this time. I had the expensive ones in it and I think with my CR, boost and Nitrous they were a little too thick.


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