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|  03-15-2013, 01:57 PM | #21 | 
| Senior Member Join Date: Apr 2012 Location: Guyton, GA 
					Posts: 1,412
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			Holy fireball....
		 
				__________________ Working on junk.... | 
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|  03-15-2013, 01:59 PM | #22 | 
| Senior Member Join Date: May 2009 Location: Charleston, SC 
					Posts: 1,489
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			It wouldn't have mattered. You would think it would, but it wouldn't. I also would have pooped myself. 
				__________________ Jaime | 
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|  03-15-2013, 02:01 PM | #23 | 
| Moderator |   
			
			There are some things that are def out of complete control, this was one of them lol.
		 
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|  03-15-2013, 02:02 PM | #24 | 
| Senior Member Join Date: May 2009 Location: Charleston, SC 
					Posts: 1,489
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			Saw pictures. Pretty f'd up. better there then on the big end for sure.
		 
				__________________ Jaime | 
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|  03-15-2013, 02:15 PM | #25 | 
| Senior Member Join Date: Jun 2008 Location: Upstate, SC 
					Posts: 2,684
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			holy shit. woot for randy still having his feet
		 
				__________________ FIRSBIRZ | 
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|  03-15-2013, 02:49 PM | #26 | 
| Senior Member Join Date: Feb 2010 
					Posts: 965
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			That was a tough 24 hour period for trucks. No body got time for slinging fluids on hot headers!  Glad she/you/everyone there is alright. 
				__________________ 12 GMC Denali HD: 4x4, 12" Bullet Proof, 24x12 American Forces, 40x15.50 Toyo M/T's, h&s mini max, deleted, 5" axle dump, S&B intake,tractions bars, air bags. 04 GMC 1500RST: TMS Iron 347/S480/4l80E - 9.63@143.22 05 GMC 2500HD: LLY@372HP/669TQ, 4x4, 8" FabTech, 4.56 gears & 37" Toyo M/T's | 
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|  03-15-2013, 03:06 PM | #27 | 
| Senior Member |   
			
			We are hell aint we rob? Converter broke in 2 pieces
		 
				__________________ I wish dupree would hurry up... | 
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|  03-15-2013, 03:19 PM | #28 | 
| Senior Member Join Date: Apr 2009 
					Posts: 1,324
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			Sucks this happened to your new ride, but it doesn't sound too costly.
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|  03-15-2013, 04:20 PM | #29 | 
| Senior Member Join Date: Jul 2011 
					Posts: 2,041
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			That was wild for sure. Luckily it wasn't during the regular dyno day with a shop full of people. I hope to see that truck back on the rollers soon, was making a bunch of power before the breakage.
		 
				__________________ [SIGPIC][/SIGPIC] | 
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|  03-15-2013, 04:54 PM | #30 | 
| Member Join Date: Apr 2012 Location: north georgia 
					Posts: 46
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			i about pissed myself...was not expecting that to happen!
		 
				__________________ 2002 L 2.6h kenne bell 783/851 Tuned by our very own Dolsvt00 bitches! Track times as soon as it cools down. | 
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|  03-15-2013, 05:14 PM | #31 | 
| Senior Member Join Date: Apr 2010 Location: Ladson,SC 
					Posts: 3,813
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			Did the converter try to lock or something? /**Sent from my iPhone5**/ 
				__________________  Dark Aladdin | 
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|  03-15-2013, 05:36 PM | #32 | 
| Senior Member |   
			
			Not that we could tell, just a bad weld on converter
		 
				__________________ I wish dupree would hurry up... | 
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|  03-15-2013, 05:38 PM | #33 | 
| Senior Member |   
			
			Its going back on very soon, probably with more boost and meth injection, i feel it will be an easy 600/700 truck and mid 10s
		 
				__________________ I wish dupree would hurry up... | 
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|  03-15-2013, 09:44 PM | #34 | 
| Senior Member Join Date: Oct 2009 Location: Ridgeville 
					Posts: 1,167
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			That was crazy to say the least. Twas an eventful night!
		 
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|  03-15-2013, 10:09 PM | #35 | |
| Senior Member Join Date: Apr 2011 
					Posts: 568
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			Those huge fireballs can be really disorienting, mine have been nitrous induced when the car got a bad case of the hook or was a lil down on power....it is actually amazing how far you can pitch a carb that was originally bolted to the intake
		 
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|  03-16-2013, 08:28 AM | #36 | 
| Senior Member Join Date: May 2008 Location: Myrtle Beach 
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			So was the convertor folks held responsible? Did they fix it right?
		 
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